Without a working Arduino Mega it is time to concentrate on reported status of the turnouts. About half of the turnouts (Wabbits) report the wrong status. Two turnouts seem to have cabling issues. The plan is to take one turnout/wabbit at a time and get everything inline.
Unicorns seem to work at intended.
Part of the fan/FanLib work kind of. Before moving on from the button functions I want to look into why the button is polled and not set up as an interrupt?
Raspberry Pi seems to have a ground/static problem. RPi shuts down randomly. At first I thought this happened when I touch a button-anything but that is not true.
Need to set up RPi to monitor traffic from the Laptop and Base Station as threads to speed up laptop to Arduino com.
Updated HelpNDoc. Norton issues again.
Can't decide if I am fixing or breaking the Wabbit configuration.
Not really liking the way pydoc generates documentation, I am looking at Sphinx if I can make it work.